(Created page with " <ul><li> No funding information provided.</li> </ul> ==Abstract== The cement production process is energy intensive both in terms of the thermal energy (firing the kiln, d...") |
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The cement production process is energy intensive both in terms of the thermal energy (firing the kiln, drying and De carbonation) and electrical energy for driving the numerous drives within the process line. The average specific power consumption of the case study plant was 111 kWh/ton of cement with an average peak demand of 9.7 MW. The high cost of electric power at 0.14 USD/kWh results in very high cost of production that significantly lowers the companys profit margin and limits its competitive advantage. The generation of electrical power from waste heat recovery would reduce the electricity power bill through partially substituting the power procured from the national grid. This research evaluated the potential that the plant has for generating electrical power from the hot waste gases vented into the atmosphere and it was found that the plant has the potential to generate 3.4 MWh of electrical power. This results to a net potential to generate 2.89 MWh of electrical power after factoring in the auxiliary power consumption by Waste heat recovery plant system at 15%. This ultimately gave a reduction of 33% in the electricity power bill of the case study plant. The paper recommends the installation of a steam rankine cycle for the power generating plant. In this work the authors designed the steam boilers for the waste heat recovery plant for conversion of thermal energy to electrical energy, selected a commercial steam turbine and evaluated its economic feasibility and established that the designed plant would have a simple payback period of 2.7 years.
The cement manufacturing process is an energy intensive industry, both in terms of thermal and electrical energy. The cost of energy keeps on fluctuating and this negatively impact on the manufacturing cost and eventually lowers the competitiveness and profitability of the cement industry. The energy costs in a cement industry account for about 26% of the total manufacturing cost of cement which is in the form of electrical energy accounting for 25% of the input energy and 75% is thermal energy [1]. Furthermore, the sources of thermal energy utilized in the cement industry are mostly nonrenewable and this necessitates deep consideration of energy conservation to guarantee sustainability.
The case study plant suffers financial loss as a result of higher per unit cost of power from the grid and the poor reliability of the supply. The poor reliability of supply negatively affects the kiln operations (the heart of operations) as a result of the sensitivity of the process to power quality resulting in high set up costs. This significantly raises the cost of production for the case study plant and eventually results in the loss of her competitive advantage.
The generation of Power from the cement kiln Waste Heat gases is an energy saving opportunity and it entails the recovery of the heat energy contained in the waste gases that are emitted into the atmosphere from the cement kiln. According to [2], the generation of Power from kiln Waste Heat Recovery is about conversion of the waste heat from the clinkering process into useful electrical energy. Cogeneration of power is achieved by utilizing this waste heat streams from the preheater and the cooler, passing the waste gases through boilers, which in turn generate steam which is used to turn/run turbines to generate electricity. The amount of heat energy recovered depends on several factors as stated by [3] namely the temperature of the waste heat gases, amount/volume of gases and thermal capacity of the waste gas, kiln system design and production capacity and the moisture content of the raw materials.
Most cement industries have not been able to generate power from waste heat recovery due to the high initial investment cost involved, the high energy requirement for drying the raw materials, in adequate technical competencies and fairly stable power cost. However, according to [4] and [5], power generations from kiln waste heat has become a very important venture in cement industry mainly due to fluctuating power costs, improvements in the economy of plant operations and the need to reduce power consumptions and finally strict environmental guidelines regarding reduction of CO2 emissions [6]. The Cost of installation is considered as the main obstacle in the installation of a waste heat recovery power plant. The High the cost of a project, the less it is feasible for investors to invest.
This paper sought to determine the potential electrical energy generation from hot waste gases from the clinkering process for the case study plant, designed steam generators for conversion of thermal energy to electrical energy and evaluated the economic feasibility of the waste heat recovery plant.
This paper focuses on determining the potential electrical energy generation from waste heat recovery through actual data measured in the plant for the volumetric gas flow rates of both the preheater and cooler exit gas streams. The paper primarily applied gas handling theories and heat transfer as a basis for the heat audit across the kiln line. The knowledge and fundamental of engineering economics was employed in determining the economic feasibility of this investment through computation of the payback period.
The case study plant has a full cement process line from mining to cement finish grinding. It has a production capacity of 1700 tons of clinker and 4000 tons of cement. The clinker produced is not sufficient to make all the required cement and therefore the plant import some clinker to meet the deficit.
The plant has undertaken several retrofitting projects in the recent past to improve operational efficiency. This includes installation of an offline pre Calciner, modification of the clinker cooler to improve on plant reliability. However, the plant still has some structural challenges that include an inefficient and short four stage preheater that limits residence time within the Calciner as well as an old cooler that limits efficient heat recovery from the cooler. The current state of the preheater limits heat transfer resulting in high gases temperatures exiting the preheater usually above (350–400)°C. This results to high specific heat consumption within the pyro processing line ranging from 900 to 950 kcal/kg clinker.
The plant is located in a relatively dry area and the raw material moisture is very low on average below 1%. This subsequently mean that the demand for drying the raw material is low and hence the high preheater exit gas temperatures has to be cooled through passing through a gas conditioning tower (GCT) before directing to the vertical raw mill and coal mill for drying the inputs. This also assists in enhancing the draught through the pyroprocessing line as the performance of the kiln induced fan improves with reduced gas temperatures.
The plant consumes on average 6.365 million units (kWh) of electrical energy per month and all of which comes from the national grid. The demand is on average 9.7 MW (peak). The average specific power consumption from mine to cement dispatch plant is 111 kWh/ton of cement. The unit cost of power is 0.14 USD resulting into an average monthly electric bill of 1 million USD as noted in the monthly power bills for the case study plant from the national power provider.
The plant produces Portland Pozzolana Cement and the product is finely ground using closed circuits ball mills to guarantee product quality with respect to achieving the target compressive strengths within a set time. The grinding department is the highest electrical energy consumer within the entire process line.
The generation of power through waste heat recovery enables the plant to reduce the electrical power bill through partially substituting the amount of power procured from the national grid. The impact of high power bills in the case study plant is depicted through
In addition, the poor reliability of power supply has negatively affected the kiln availability as a result of the sensitivity of the process to power quality. The heat up cost and the thermal shocks suffered by the kiln whenever there is a power outage and or a dip has over the years cost the plant huge sums of money both in terms of fuel (heating up-process set up) and refractory replacement (failure rate is high because of thermal shocks). Power interruptions constitute a plant downtime of an average 2% of total production time per annum.
It was in light of the above bottlenecks currently faced by the case study plant that the generation of power through waste heat recovery was considered a very prudent and economically viable project. It enables the plant to substitute 32.68% of its total electric power consumption and reduce the power bill by an equal margin. It also improves kiln reliability, as the power generated from waste heat recovery is sufficient to keep the sensitive part of the kiln running and cushioned from frequent power interruptions from the grid.
The volumetric flow rates of the waste heat gas streams from the cooler exhaust and the preheater exit were measured as well as their operating conditions like temperatures and the static pressures. The determination of the volumetric flow rate required the knowledge of the density of the gas stream, dust concentration, the gas temperature, the barometric pressure, and duct cross section area and gas velocity. The computation of the gas density was based on the measured volumetric gas composition. The process instruments that were used in the determination of the waste gases volumetric flow rates were Pitot tubes and “S” tube, Flue Gas Analyzer (O2, SO2, N2 and CO). The velocity of the gas stream was calculated from the Bernoullis principle.
|
(1) |
where U = Gas Velocity; Pt = Total pressure; Ps = Static pressure; r = Gas Density.
Solving for velocity U after rearranging gives
|
(2) |
The calculated mean square velocity was multiplied by the duct cross-sectional area to get the actual volumetric flow rates. The flow rates were normalized at standard conditions and the process was repeated over a two month period and eventually an arithmetic average volumetric flow rate calculated for the two gas streams. The average measured volume of gases was 130,269 Nm3/h at 383°C and 132,021 Nm3/h at 332°C for the kiln preheater and the cooler, respectively. The results are shown in Tables A7 and A8 in the Appendices 6 and 7.
The thermal energy analysis of the cooler exhaust waste gas stream was conducted and it was found that it contains 784 kJ/kg clinker of thermal energy per hour, which translated to 187.25 kcal/kg clinker per hour at 332°C as shown in Table A9 in the Appendix 8.
The volumetric flow rate of the preheater exit gases, characterization parameters, measured gas composition and their respective thermodynamic properties were utilized in the determination of the thermal energy content of the gases exiting the preheater tower. The mean specific heat capacity of the gas stream were calculated as per the expression below and applied to the computation of the composite specific heat capacity as per the measured volumetric gaseous composition. That is,
|
(3) |
where a, b, c, d are given thermodynamic values for different gases and materials at various temperature ranges and Cpm is the mean heat capacity. This is the expression for calculation of Cp mean of gases between temperature T and a reference temperature to [7].
The thermal energy analysis of the preheater exit gases found out that it contained 756 kJ/kg clinker of thermal energy per hour, which translated to 180.5 kcal/kg clinker per hour. The results are summarized in Table A1 in Appendix 1.
The preheater exit gases are passed through a GCT to lower the temperature before they can be directed to the raw mill and coal mill for drying the raw materials and passed through a bag filter for dust trappings. The hot exhaust gases enter the top section of the vertical, cylindrical-shaped and insulated tower for cooling by water injection as shown in Figure 1. The gases are drawn through the conditioning tower by a centrifugal fan.
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Figure 1. Schematic picture of the gas conditioning tower and water spray control mechanism. |
A heat balance across the GCT was conducted and the preheater exit gases and injected water were considered as heat input to the system, whereas the GCT exit gases, the GCT bottom dust and the latent of vaporization considered as heat output.
The net thermal energy from the preheater waste gases available for power generation was the balance after accounting for the heat requirement for drying of the raw material during the grinding Process as well as for drying the coal fuel. The summarized results for the heat balance are as shown in Table A2 in the Appendix 2.
The heat balance results in Table A2 demonstrated that 92.9 kcal/kg of clinker per hour is currently used in cooling the preheater exit gases by heat transfer into the water being injected into the GCT. The preheater waste heat recovery system is meant to utilize this heat energy by bypassing the GCT and passing this gas stream through a steam generator for power generation.
According to [8], the location of the preheater boiler is at the outlet of the preheater and the gas that has passed the steam boiler is returned to the existing gas duct. The best practice is to install inlet dampers into the preheater boiler that can be used for adjusting the gas volume to the Preheater boiler. The Figure 2 shows a design in which the cooler vent gases and the preheater exit gases generate steam in separate boilers that feed into one steam turbine and generator. The steam flows to a steam turbine, where it expands by decompression and thus drives a generator [9]. In the condenser the steam is cooled, condensed back to water in a recooling system and again pumped to the steam generator.
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Figure 2. Rankine cycle-detailed sample schematic sketch. |
It was found out that the plant had a gross capacity to cogenerate 3.4 MWh, which resulted to a net production of 2.89 MWh after accounting for the auxiliary power consumption of the waste heat recovery plant. According to [3], the efficiency of the steam turbine process is around 25–30%, meaning only a 1/4 of the waste heat is transformed into electrical energy in the cement industry.
The thermal energy content of cooler waste gases was found to be 784 kJ/kg of clinker. However, only 435 kJ/kg of clinker can be utilized for power generation. This is because the cooler boiler in the waste heat recovery plant is not 100% and the flue gases exits the cooler boiler at a temperature of 150°C. This wasted heat can be utilized by enhancing the efficiency of the cooler boiler through increasing the surface area for heat transfer (increases the capital investment) and effective lagging of the heat transfer area to minimize heat loss through conduction and radiation from the boiler surfaces.
The thermal energy balance across the preheater and cooler steam generator gave a steam production capacity of 9.744 and 10.853 tons/h for preheater and cooler boiler, respectively, at a temperature of 230°C and a pressure of five bars. The steam parameters of five bars and 230°C were based on the suitability of a commercial low parameter steam turbine (model S3-05) that was selected for the waste heat recovery plant [10].
Conducting a material balance around the boiler equipment required the definition of the system boundary. The system boundary constitutes inputs, namely; Flue gases (kg/h), raw feed water (kg/h). The output constitutes steam, which is the fundamental energy carrier (working fluid), the trapped dust constituting of the drain from the boiler bottom drum, wall losses and flue gases exiting the boiler.
The main features of the boiler include the economizer, the evaporator and the super heater according to [9]. The economizer is used to recover heat from the exit gas from the boiler to reduce the temperature of flue gas before venting into the atmosphere. The heat transfer is more effective if the economizer surface is large. The purpose of the evaporator is basically changing the phase of water from liquid to vapor, that is, evaporation. The generated steam is then transferred to the steam drum for steam/water separation by difference in density and the vapor is then transferred to the super heater. The purpose of the super heater is to provide the heat to increase the steam temperature to above saturation temperature. The heat input to the super heater is from hot flue gas as the flow arrangement is countercurrent to the flow of the working fluid for optimal heat transfer [11]. The designed waste heat recovery boiler flow diagram is shown in Figure 3.
The computation of heat transfer surface areas required the heat transfer coefficient and the temperature differences (inlet and outlet) between the streams as per the expression below.
|
(4) |
= heat to steam, kW (thermal power) which was calculated from the steam boiler heat balance [1, 3, 4, 12].
Where k = heat transfer coefficient, W/m2 K; = logarithmic temperature differences; A = Required surface area, m2.
There are three modes of heat transfer that occurs inside and outside the steam generator which involve convection, radiation and conduction and mixed heat transfer at the boundary conditions.
|
(5) |
This is the expression for getting the logarithmic temperature difference for a counter flow system where Tgi = Flue gas inlet temperature; Tso = Steam out temperature; Tgo = Flue gas outlet temperature and Tsi = Steam in temperature. The calculated heat transfer areas for the two boilers were calculated and summarized in Tables A4 and A5 for cooler and preheater boiler, respectively, in the Appendix 4.
The simple Payback analysis was used to determine the amount of time expressed in years, required to recover the first cost of this project [12]. The payback period was an estimated time for the revenues in terms of fuel savings, reduced electricity bill as well as the increase in clinker output to completely recover the initial investment. The fuel savings are a result of reduced consumption of heavy furnace oil (HFO) and coal (thermal fuels) for plant set up after a power interruption. The plant set up involves preheating the kiln system to achieve the required operating temperatures for the clinkering process. According to [13], Operating & Maintenance costs for a 1–5 MW waste heat recovery plant ranges from $0.005 to $0.020/kWh and reflect the wide range of maintenance requirements that might be experienced. The total initial investment cost of USD 2.5 million per MW was used as recommended by [14] as well as from [15]. The auxiliary power requirement of (10–15)% of gross power generation is factored in arriving at the net power generation from the waste heat recovery power plant [[[#ese3153-bib-0014|[14]]]. The simple payback period for this project based on electrical and thermal savings worked out to be 2.69 years as shown in Table A6 in Appendix 5
The volumetric flow rate of the cooler and preheater exhaust gas streams was measured and thermal dynamic balance carried out to quantify the thermal energy content. The potential electrical energy that could be generated from exhaust gas streams by conversion through a Steam rankine cycle was evaluated. A heat audit was done and several heat balances carried out for the new plant layout to quantify the thermal energy content in the waste gases steam that could be recovered for power generation.
It is noted that not all gasses from the preheater exit is available for power generation as some was reserved for raw material and fuel drying. The paper focused on recovering the heat previously lost in the GCT. The paper focused on recovering the heat previously lost in the GCT. The source of thermal energy to run the waste heat recovery Power plant was purely the waste gases from the kiln and there is no other source of thermal energy that was considered in this research work.
This paper established that the hot waste gases being vented into the atmosphere from the clinkering process at the case study plant have a net potential to generate 2.9 MWh of electrical power from waste heat gas recovery which was sufficient to meet 33% of the plants electric power demand. The designed steam generators’ gave a total steam production capacity of 20.6 tons/h at a pressure of five bars and at 230°C. The required capital investment for the installation of this project was Ksh 875,500,000 with a simple payback period of 2.7 years which was considered quite attractive.
A commercial low parameter steam turbine (model S3-05) to suit the calculated optimum conditions of five bars and 230°C was selected for the waste heat recovery plant as per the data given in Appendix 4 [12].
None declared.
Measured specific thermal energy | |
---|---|
Preheater gas stream | 756 kJ/kg clinker |
Cooler gas stream | 784 kJ/kg clinker |
Heat input | Heat output | ||
---|---|---|---|
Flue gas into GCT | 180.4 kcal/kg clinker | Flue gas exit | 92.6 kcal/kg clinker |
Feed Water | 6.9 kcal/kg clinker | Heat consumed by water | 92.9 kcal/kg clinker |
GCT solid discharge collected at the bottom by a screw conveyor. | 0.8 kcal/kg clinker | ||
Wall losses | 1.0 kcal/kg clinker |
Potential electrical energy generation | |
---|---|
Thermal energy of preheater waste gases | 756 kJ/kg clinker |
% Heat requirement for drying | 51.3% |
Heat requirement for drying | 388 kJ/kg clinker |
Remainder for Power generation | 368 kJ/kg clinker |
Thermal energy in Cooler waste gases | 784 kJ/kg clinker |
Thermal energy in cooler boiler exit gases at 150°C | 350 kJ/kg clinker |
Thermal Energy Available for cogeneration from cooler waste gases | 434 kJ/kg clinker |
Total thermal energy available for electrical heat generation | 802 kJ/kg clinker |
Recovery Efficiency | 0.2 |
Power generated | 160.4 kJ/kg clinker |
48.13 kWh/ton of clinker | |
Plant clinker capacity | 70 tons/h |
Total Gross potential power generated | 3400 kWh |
3.4 MWh | |
Auxiliary power consumption (by WHR system @15%) | 0.505 MWh |
Net Potential Power Generation | 2.89 MWh |
Cooler boiler | |||
---|---|---|---|
Economizer | Evaporator | Super heater | |
Heat to steam (Φ; kW) | 574 | 519.9 | 962 |
Heat transfer coefficient (K; W/m2 K) | 453 | 246.0 | 205 |
Temperature difference (∆Tlm) | 33 | 72.1 | 121 |
Heat transfer surface (m2) | 38 | 29.3 | 38.8 |
Preheater boiler | ||
---|---|---|
Evaporator | Super heater | |
Heat to steam (Φ; kW) | 763.8 | 1107.3 |
Heat transfer coefficient (K; W/m2 K) | 127 | 542 |
Temperature difference (∆Tlm) | 135 | 154 |
Heat transfer surface (m2) | 44.5 | 13.3 |
Waste heat recovery (WHR) payback calculations | ||
---|---|---|
Exchange rate, Ksh to USD | 103 | |
Operating days per year | 300 | |
Tph, clinker | 71 | |
Historical Stop hrs due to power/month | 14 | |
Kenya power supplied unit cost | 14 | Ksh/kWh |
Item Description | Value | Units |
Cost of WHRS per MW | 2.5 | Million USD |
Gross Waste heat recovery potential | 3.4 | MW |
Net power generation (85% of gross) | 2.89 | MW |
Project cost estimates | 875,500,000 | Ksh |
Expected net generation annually | 20,808,000 | kWh |
Expected generation per month | 1,734,000 | kWh |
Operating costs | 0.02 | USD per kWh |
Total operating costs | 50,428,800 | Ksh |
Revenues | ||
Annual Savings through improved specific power consumption(Reduced set up costs associated with firing the kiln with nil production due to persistent power interruptions | 5,655,000 | Set up costs |
Cost of units substituted from national grid | 291,312,000 | Ksh |
Lost opportunity, pa on clinker production (Clinker not produced due to plant unavailability due to power interruption) | 78,750,000 | Ksh |
Total annual revenues | 375,717,000 | Ksh |
Net revenue annually (less Operation cost) | 325,288,200 | Ksh |
Simple pay back in years | 2.69 |
Date | Preheater exhaust gases, Nm3/h | Temperature (°C) | Date | Preheater exhaust gases, Nm3/h | Temperature (°C) |
---|---|---|---|---|---|
17/11/2015 | 136,320 | 381 | 8/12/2015 | 130,394 | 387 |
19/11/2015 | 130,294 | 380 | 10/12/2015 | 128,477 | 372 |
24/11/2015 | 131,406 | 388 | 12/12/2015 | 127,681 | 374 |
27/11/2015 | 130,032 | 390 | 16/12/2015 | 127,029 | 371 |
28/11/2015 | 123,872 | 390 | 17/12/2015 | 130,741 | 370 |
30/11/2015 | 138,902 | 382 | 18/12/2015 | 126,874 | 376 |
2/12/2015 | 137,543 | 388 | 19/12/2015 | 132,063 | 379 |
4/12/2015 | 127,679 | 383 | 20/12/2015 | 126,051 | 371 |
6/12/2015 | 129,673 | 384 | Average | 130,296 | 383 |
Date | Cooler exhaust gases, Nm3/h | Temperature (°C) | Date | Cooler exhaust gases, Nm3/h | Temperature (°C) |
---|---|---|---|---|---|
17/11/2015 | 129,540 | 350 | 8/12/2015 | 127,090 | 378 |
19/11/2015 | 132,896 | 331 | 10/12/2015 | 129,442 | 365 |
24/11/2015 | 133,628 | 316 | 12/12/2015 | 126,436 | 345 |
27/11/2015 | 128,220 | 320 | 16/12/2015 | 127,243 | 344 |
28/11/2015 | 128,991 | 376 | 17/12/2015 | 129,281 | 324 |
30/11/2015 | 132,412 | 380 | 18/12/2015 | 126,207 | 335 |
2/12/2015 | 127,353 | 303 | 19/12/2015 | 127,229 | 350 |
4/12/2015 | 129,045 | 320 | 20/12/2015 | 129,624 | 325 |
6/12/2015 | 131,234 | 335 | Average | 132,021 | 332 |
Cooler exhaust heat energy content | |||
---|---|---|---|
Volume measured | 126,463 Nm3/h | Mass flow rate of gases | 162,194.7 kg/h |
Temperature of the gas, °C | 332 | ||
Clinker production | 71,000 kg/h | Enthalpy of the gas | 82.0 kcal/kg |
Ambient temperature, °C | 26 | Thermal energy of cooler waste gases | 13,299,912.9 kcal/h |
Altitude above sea level, m. | 1532 | 55,686,735.3 kJ/h | |
Atmospheric pressure, hPa | 856 | ||
Ambient relative humidity, % | 50% | Thermal energy per unit clinker production | 187 kcal/kg clinker |
Humidity calculations | 784 kJ/kg clinker | ||
Absolute humidity, kg H2O/kg dry air | 0.012719364 | ||
Air moisture by mass, % | 1.26% | Thermal energy of cooler boiler exhaust gases per unit clinker production at 150°C | 83 kcal/kg clinker |
Air moisture by volume, % | 2.00% | 350 kJ/kg clinker | |
Wet molecular weight, g/gmole wet air | 28.75 | Thermal energy available for power generation | 435 kJ/kg clinker |
NO. | Model | Capacity (MW) | Speed (r/min) | Inlet | Exhaust pressure (MPa) | Weight (t) | Overall dimensions L × W × H (mm) | ||
---|---|---|---|---|---|---|---|---|---|
Pressure (MPa) | Dryness () | Temp () | |||||||
1 | S1.0-0.3 | 1 | 3000 | 0.3 | 200 | 0.008 | 14.6 | 3220 × 2150 × 1750 | |
2 | S1.3-0.36 | 1.3 | 3000 | 0.36 | 180 | 0.013 | 18.2 | 4550 × 2300 × 2600 | |
3 | S1.5-0.14 | 1.5 | 3000 | 0.14 | 0.995 | 0.0072 | 18.7 | 3200 × 2300 × 2532 | |
4 | S1.5-0.16 | 1.5 | 3000 | 0.16 | 0.995 | 0.0088 | 18.7 | 3200 × 2300 × 2532 | |
5 | S1.5-1.7 | 1.5 | 3000 | 1.7 | 240 | 0.098 | 9.8 | 4120 × 2650 × 2530 | |
6 | S2-0.6 | 2 | 3000 | 0.6 | 275 | 0.0061 | 12 | 4257 × 2145 × 2375 | |
7 | S2.6-1.08 | 2.6 | 3000 | 1.08 | 0.995 | 0.009 | 17.7 | 3500 × 2850 × 2500 | |
8 | S3-0.5 | 3 | 3000 | 0.5 | 0.995 | 0.009 | 16 | 3250 × 2850 × 2500 | |
9 | S3-0.5 | 3 | 3000 | 0.5 | 230 | 0.009 | 16 | 3250 × 2850 × 2500 | |
10 | S3-0.5 | 3 | 3000 | 0.5 | 270 | 0.008 | 15.7 | 3500 × 2250 × 1750 | |
11 | S3.69-1.27 | 3.69 | 3000 | 1.27 | 300 | 0.007 | 17.7 | 3500 × 2850 × 2500 | |
12 | S3.9-1.08 | 3.9 | 3000 | 1.08 | 0.995 | 0.009 | 17.7 | 3500 × 2850 × 2500 | |
13 | S4-0.5 | 4 | 3000 | 0.5 | 230 | 0.01 | 16.3 | 3300 × 2840 × 2500 | |
14 | S5-1.0 | 5 | 3000 | 1 | 260 | 0.01 | 17.9 | 3510 × 2830 × 2485 | |
15 | S6-0.5 | 6 | 3000 | 0.5 | 230 | 0.01 | 38.1 | 5000 × 3900 × 2610 | |
16 | S6-0.5 | 6 | 3000 | 0.5 | 0.995 | 0.01 | 38.1 | 5000 × 3900 × 2610 | |
17 | S6-1.0 | 6 | 3000 | 1 | 230 | 0.009 | 42.1 | 5160 × 3900 × 2600 | |
18 | S6-1.0 | 6 | 3000 | 1 | 0.995 | 0.01 | 42.1 | 5160 × 3900 × 2600 | |
19 | S8-1.0 | 8 | 3000 | 1 | 260 | 0.01 | 42.9 | 5160 × 3900 × 2600 | |
20 | S8-1.0 | 8 | 3000 | 1 | 0.995 | 0.01 | 42.9 | 5160 × 3900 × 2600 | |
21 | S9-1.35 | 9 | 3000 | 1.35 | 310 | 0.005 | 43.2 | 5190 × 3900 × 2600 | |
22 | S10-0.981 | 10 | 3000 | 0.981 | 300 | 0.008 | 43.9 | 5200 × 3900 × 2600 | |
23 | S10-1.0 | 10 | 3000 | 1 | 260 | 0.01 | 43.8 | 5160 × 3900 × 2600 | |
24 | S10-1.0 | 10 | 3000 | 1 | 0.995 | 0.01 | 43.9 | 5160 × 3900 × 2600 | |
25 | S12-0.785 | 12 | 3000 | 0.785 | 415 | 0.0073 | 45 | 5205 × 3770 × 2450 | |
26 | S12-1.0 | 12 | 3000 | 1 | 0.995 | 0.01 | 42.9 | 5160 × 3900 × 2600 | |
27 | S12-1.25 | 12 | 3000 | 1.25 | 315 | 0.01 | 39.1 | 4910 × 3900 × 2600 |
Published on 01/06/17
Submitted on 01/06/17
Licence: Other
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